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- Rocket motor cases and the specially designed production equipment therefor. 四、火箭发动机的壳体及为其专门设计的生产设备。
- Using pintle technology, a conventional solid propellant rocket motor can provide variable thrust levels, increasing the energy utilizing efficiency and improving the capability of the missile. 喉栓式变推力发动机可实现固体火箭发动机的推力调节,提高能量利用效率,从多方面提升导弹武器的作战效能,因此具有强烈的军事需求。
- Four nozzles, canted outboard, split the exhaust of the solid rocket motor into four equal tails. 四个向外倾斜的喷管把固体火箭发动机的排气流分成四个相等的尾巴。
- There is a rocket motor on the satellite by which the direction of the satellite can be changed if necessary. 在卫星上还有一个火箭马达,必要时可以用它来改变卫星的方向。
- Rocket motors have many advantages over other forms of propulsion. 火箭发动机比其他推进器有许多优点。
- According to the requirement of pasty propellant rocket motor, a composite plasma igniting plan was adopted. 摘要根据膏体推进剂火箭发动机。
- Motor efficiency can be increased through the use of improved materials, improved heat transfer, more sophisticated control and by cleverer motor designs and configurations. 提高电机效率可以通过许多途径,包括采用改良了的材料、改进后的热传递、更复杂的控制系统,也可以通过更合理的结构和设计。
- The influence of structure axial vibration on the internal ballistics of solid rocket motor was investigated. 文中研究了固体发动机结构的轴向振动对燃烧室内弹道性能的影响。
- This paper analyzes the motor efficiency test and evaluation methods in detail, and introduces the constitution and hardware principles of test platform. 详细分析了电动机能效试验及评价方法,介绍了节能电动机试验平台的组成及硬件原理。
- Investigated charring erosive characters of internal insulation of solid rocket motor under flight acceleration. 研究了固体火箭发动机内绝热层在飞行加速度条件下的炭化烧蚀特性。
- An experimental burst diaphram of 0.011" brass shim stock, installed at the nozzle entrance to increase motor efficiency, caused an overpressurization of the motor. 实验水管爆裂,连续的0.;011 “黄铜沉股票,安装在喷嘴的入口,以增加电动机的效率,造成了overpressurization的汽车。
- The thrust vector control(TVC) performance test of solid rocket motor is presented in this paper. 本文介绍了固体火箭发动机水下推力矢量特性试验。
- A response surface method(RSM) for structure reliability analysis of solid rocket motor(SRM) grain was presented. 发展了一种固体火箭发动机药柱结构可靠度分析的响应面法。
- The preliminary design data for the k APPA-DX rocket motor is presented in this web page. 初步设计数据的K appa -的DX火箭发动机是在这方面的网页。
- Buckling analysis on rear dome of solid rocket motor case was studied by means of ANSYS. 用ANSYS软件对固体发动机壳体后封头进行了外压屈曲分析。
- Crose J G.Reliability of solid rocket motor cases and nozzles[R].NTI S,N93-22103. 王松柏.;固体火箭发动机壳体结构的动态可靠性设计[J]
- Finite element method is used in the study of nozzle damping of instable combustion in a solid rocket motor. 应用有限单元法研究固体火箭发动机不稳定燃烧中的喷管阻尼,并用波衰减对比法进行了试验研究。
- In use, with the flow, changes in lift, submersible pump motor efficiency and a corresponding change in power, the use of submersible pump of the economy and have a certain impact on reliability. 使用中,随着流量、扬程发生变化,潜水电泵的效率和电动机功率也相应发生变化,对潜水电泵使用的经济性和可靠性有一定的影响。
- Carbon/carbon composites have become the most ideal materials for nozzles of solid rocket motor (SRM). 摘要C/C复合材料已成为固体火箭发动机(SRM)最理想的喷管材料。
- Space debris made news on March twelfth when a part of an old rocket motor about ten centimeters in size threatened the International Space Station. 空间碎片在三月二十日那天就制造了一个新闻:一个大约十厘米大小的旧火箭马达威胁着国际空间站。